My RX7 FD3S Re-Amemiya Twin Turbo Build
#156
Well duty calls and i wont be able to finish the car this weekend
I have to help out some of friends at Simply Clean 4 out in Orlando, FL
But shes just about ready to start
got everything for the fuel system, so i'll be putting that all together on sunday
and also modifying the oil drain line from the top turbo which i found was touching the manifold
then my engine builder will be coming to the house sometime next week to plug up the wiring harness and starting her up
hopefully i'll get to tune her on friday of next week!!
got to take some motivational pics today that i thought i'd share with you guys lol
I have to help out some of friends at Simply Clean 4 out in Orlando, FL
But shes just about ready to start
got everything for the fuel system, so i'll be putting that all together on sunday
and also modifying the oil drain line from the top turbo which i found was touching the manifold
then my engine builder will be coming to the house sometime next week to plug up the wiring harness and starting her up
hopefully i'll get to tune her on friday of next week!!
got to take some motivational pics today that i thought i'd share with you guys lol
#157
finally have some updates for you guys!!
well good and bad updates sadly
the good is that the motor is all put back together...
i ran into a massive oil leak because of the rear oil return flange on the block, turns out there was an edge there i couldnt see and the flange ending up resting on the flange and didnt seal against the block, so i had to grind down an excessive edge on the flange and put it back together...everything is perfect with that now
I also made my first attempts at starting which didnt work LOL!! didnt really expect more than that though lol
it sounds like the motor is flooded so i'm going to pull the EGI fuse and turn it over a couple times to get rid of the excess fuel, clean up the plugs and give it another shot tomorrow
PICS AND VIDEO!!
the last pic of just the exhaust smoking which was pretty cool lol
well good and bad updates sadly
the good is that the motor is all put back together...
i ran into a massive oil leak because of the rear oil return flange on the block, turns out there was an edge there i couldnt see and the flange ending up resting on the flange and didnt seal against the block, so i had to grind down an excessive edge on the flange and put it back together...everything is perfect with that now
I also made my first attempts at starting which didnt work LOL!! didnt really expect more than that though lol
it sounds like the motor is flooded so i'm going to pull the EGI fuse and turn it over a couple times to get rid of the excess fuel, clean up the plugs and give it another shot tomorrow
PICS AND VIDEO!!
the last pic of just the exhaust smoking which was pretty cool lol
#161
got the headlight finally...the only lamp i found that i really like and still gives me enough room on the inside of the headlight bucket to run my ducting to the turbos she looks so mean!!
#162
well what can go wrong did go wrong...
Lost the compression on the rear rotor, dropped all the way down to 40 psi
its so weird, the motor was running really strong and well everytime i started it up and let it idle at my house...then the first time we start it up at the tuners shop, no compression on the rear rotor...
nothing changed at all from when we had it at my house, to when we got there...so strange
heres some pics of the drive up there and a video of what she sounded like when we were there
Lost the compression on the rear rotor, dropped all the way down to 40 psi
its so weird, the motor was running really strong and well everytime i started it up and let it idle at my house...then the first time we start it up at the tuners shop, no compression on the rear rotor...
nothing changed at all from when we had it at my house, to when we got there...so strange
heres some pics of the drive up there and a video of what she sounded like when we were there